kentmcn

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kentmcn
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  • Pressing the Reset button on the controller board allowed the connection to complete and maintain. I was still unable to use Manual Control on R-H. Then I noticed their were three printers, with two of them using the same API key. Getting a new key…
  • Problem solved: I noticed that there was a slight difference in the planes of the two boards (Mega 2650 and RAMPS), such that the pins connecting the boards were further apart at the top (Aux header) than at the bottom. Tightening the screw at the …
  • M119 shows all endstops are low. STEPPER_HIGH_DELAY and DOUBLE_STEP_DELAY are both changed to '1' as you suggested. Same situation: Y moves OK. X doesn't move. The X leadscrew is limp (turns freely) after a move command. Z doesn't move. The Z lea…
  • After removing the stepper drivers, the !ENABLE voltages are: X=4.89; Y=0.0009; Z=0.001. After attempting moves (with the stepper drivers missing) they are: X=4.89; Y=0.0009; Z=4.88. I have a (nearly) identical setup handy, which I've uploaded the …
  • Hi Don, Thanks for the response. M119 reports Xmin:L Xmax:L Ymin:L Ymax:L Zmin:L Zmax:L All the end_stops are set to inverting=true, as are the end_stops themselves and the pullups(=true). I set them all to INVERTING=false and m119 reports the…